Alrighty.. now that i finished work i can do a proper update.
So sunday went to a meet, that was good. First drive with the new exhaust on and holy sh*t its good. So much better then the loud one. Nice and quiet when im just puttin around but when i get on boost i have the screamer come in to play so atleast it sounds good
Really happy with how its been driving and no issues have came up.
Heres some pics from that..




Then on wednesday i had a track day at Queensland Raceway. It was awesome. First session on the sprint track was getting use to the car but it felt really good so managed to get a 63.4 on the last lap

. Second session i was a bit more confident and had no traffic so it gave me more room to improve and that i did. Managed a 62.3. Stoked with those times. Car is pretty easy to control. On exits i need to be careful cos it does wanna get a bit sideways there but in saying that its really easy to control sideways and isnt snappy like i was expecting. Brakes seemed to do the job pretty good (nb8a brakes with solid rotors and xp10's all round) and it never really felt like they were wearing that much. Tires held up really good but towards the end of the sessions i was getting a bit of understeer so maybe just a bit hot? not sure.
Next was clubman circuit and i never really got the hang of it.. A few corners i ran a bit wide and ended up with a bit of oversteer because of that but given more track time i think i will improve.. Once again brakes did there job as well as tires. After the first session i got a 65.4 i think. Second session the car felt a bit twitchy and i wasnt sure why so i only lapped in 66's but upon coming to the pits one of the bushings fell out of the lower control arm on the outers

So that could explain it haha. Temps throughout the day were spot on. Never looked like over heating
Apart from the bushing falling out, (two on closer inspection and two more were on its way out) the only other issue i had was from the breather. because the catch can doesnt route back to the intake or some other place i was getting a bit of oil and as it built pressure inside the can it would expell into the engine bay. There was a fair bit of blowby but ive had it looked at with the mechanics and its nothing to worry about. Once a proper breathing system is put in place i shouldnt have any issues at all..
So today the local mx5 parts warehouse had some lower control arms all with sperical bushings in them. Since i was down a bushing i decided to chuck them in and be done with it. I needed another alignment anyways. Next week ill hopefully get the tune looked over at gt auto to make sure its all running the way it should. Im deciding not to drive to sydney this weekend as its just to much and ive got to much work on atm. And ive realised after the track day, that power is perfectly fine for learning with. If i got anymore power id definitely have issues with brakes and tires.
So next track day is hopefully the 20th at qr again only on sprint track this time. Hopefully i can sort out the tune, breathing before then

Would have to say this is the most fun ive had in this car yet
Pics:
Cruising out

Trying to catch the s2k on the straight

Got him

One last one

Cheers

NA6 - Longnose engine, JR cai, full custom exhaust, BC coilovers, NA8 front brakes, frog arms, cusco cage, secret element tie rods